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JGA12-N20 DC Motor: Problem Analysis and Solutions

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JGA12-N20 DC Motor: Problem Analysis and Solutions

June 18, 2025

JGA12-N20 DC Motor: Problem Analysis and Solutions

In the field of miniature motors, the JGA12-N20 DC motor stands out for its compact size and robust performance, making it a preferred choice across various industries. However, during practical applications, the R&D team encountered several issues that significantly impacted product performance and user experience. Through in-depth analysis and optimization, these issues were effectively resolved.

I. Background

The company aimed to develop smart devices to meet market demands for efficient, convenient, and low-noise equipment. However, during early product testing, the team found that traditional DC motors generated excessive noise and had unstable torque output under high loads, affecting device performance and user experience. To address these issues, the team sought a high-performance miniature DC motor and ultimately selected the JGA12-N20.

II. Problem Description

(1) Noise Issue

During operation, the motor produced high noise levels, particularly at low speeds. This not only affected user experience but also caused noise pollution in residential environments.

(2) Unstable Torque Output

Under high loads, the motor's torque output fluctuated significantly, resulting in unstable device operation. This not only reduced operational efficiency but also led to potential long-term mechanical failures.

(3) Heat Dissipation Issue

After prolonged operation, the motor's temperature rose, affecting device stability and lifespan. This was especially problematic during high-frequency use, potentially triggering overheating protection shutdowns.

III. Problem Analysis

(1) Noise Issue

The noise primarily originated from the meshing of internal gears and vibrations of the motor housing. At low speeds, the meshing frequency was lower, but each meshing event released significant energy, amplifying noise.

(2) Unstable Torque Output

The unstable torque output was likely due to an imprecise control algorithm, causing significant current fluctuations when the load changed, thereby affecting torque delivery. Additionally, there might have been design flaws in the motor's gear transmission system, leading to uneven torque transfer.

(3) Heat Dissipation Issue

Poor heat dissipation was likely due to inadequate cooling design in the motor, preventing heat from being effectively dissipated. As a result, the internal temperature of the motor increased during extended operation, impacting its performance and longevity.

IV. Solutions

(1) Noise Optimization

  1. Gear Design Improvement: Replaced spur gears with high-precision helical gears to optimize the gear meshing angle and reduce noise during meshing.
  2. Sound-Insulating Materials: Added sound-insulating materials, such as rubber pads or sound-absorbing sponges, inside the motor housing to absorb noise generated during operation.
  3. Motor Installation Optimization: Ensured that the motor was securely fastened during installation to reduce housing vibrations, thereby lowering noise levels.

(2) Enhancing Torque Stability

  1. Control Algorithm Optimization: Implemented a closed-loop control algorithm to monitor the motor's current and torque output in real-time and automatically adjust operating parameters according to load changes to ensure stable torque delivery.
  2. Torque Compensation Module: Integrated a torque compensation module into the motor control system to dynamically compensate for torque output through software algorithms, reducing torque fluctuations during startup and shutdown.

(3) Heat Dissipation Optimization

  1. Heat Sink Addition: Installed heat sinks on the motor housing to increase the surface area for heat dissipation and improve cooling efficiency.
  2. Internal Structure Optimization: Redesigned the air flow channels inside the motor to add ventilation holes, ensuring effective heat dissipation during operation.
  3. Thermal Conductive Materials: Applied thermal conductive silicone to key components inside the motor to quickly transfer heat to the housing, further enhancing cooling performance.

V. Implementation Results

(1) Noise Reduction

After optimization, the motor's operating noise was reduced from 50 decibels to 35 decibels, significantly improving the user experience and reducing noise pollution in residential settings.

(2) Enhanced Torque Stability

Torque output stability was improved by 30%, resulting in a smoother device operation and a noticeable increase in operational efficiency. The long-term stability of the motor was also enhanced.

(3) Improved Heat Dissipation

The motor's operating temperature was reduced by 20%, eliminating instances of overheating and automatic shutdown, and significantly enhancing the device's continuous operation capability.

VI. Conclusion

By addressing the noise, torque stability, and heat dissipation issues of the JGA12-N20 DC motor, the R&D team successfully resolved the practical problems encountered in application, significantly enhancing the performance and user experience of the device. These improvements not only solved the immediate issues but also provided valuable insights for similar application scenarios. Looking ahead, with continuous technological advancements, the JGA12-N20 motor is expected to play a significant role in more fields, bringing greater convenience and innovation to people's lives.
Contact Details
Shenzhen Jinshunlaite Motor Co., Ltd.

Contact Person: Mrs. Maggie

Tel: 15818723921

Fax: 86--29880839

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