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A58-3650 DC Motor: Problem Analysis and Solutions

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A58-3650 DC Motor: Problem Analysis and Solutions

June 19, 2025

A58-3650 DC Motor: Problem Analysis and Solutions

In smart home devices, a high-performance DC motor is crucial for intelligence. A smart home company used the A58-3650 DC motor in its new smart curtains, boosting product performance and user experience. However, during application, the R&D team encountered issues that impacted product performance and user experience. After thorough analysis and optimization, these issues were effectively resolved.

I. Background

The company aimed to develop smart curtains for efficient, convenient, and low-noise devices. Early tests showed traditional DC motors were noisy and had unstable torque under high loads, affecting device performance and user experience. To address these issues, the company chose the A58-3650 DC motor.

II. Problem Description

(1) Noise Issue

The motor produced high noise, especially at low speeds, affecting user experience and potentially causing noise pollution in homes.

(2) Unstable Torque Output

Under high loads, the motor's torque output fluctuated, resulting in uneven curtain opening and closing. This affected device efficiency and could lead to long-term mechanical failures.

(3) Heat Dissipation Issue

After prolonged operation, the motor's temperature increased, affecting device stability and lifespan. This was especially problematic during high-frequency use, potentially triggering overheating protection shutdowns.

III. Problem Analysis

(1) Noise Issue

The noise primarily originated from the meshing of gears inside the motor and vibrations of the motor housing. At low speeds, the meshing frequency was lower, but each meshing event released significant energy, resulting in more noticeable noise.

(2) Unstable Torque Output

The instability in torque output was likely due to an imprecise control algorithm that caused significant current fluctuations when the load changed, thereby affecting torque delivery. Additionally, there might have been design flaws in the motor's gear transmission system that led to uneven torque transfer.

(3) Heat Dissipation Issue

The poor heat dissipation was probably due to inadequate cooling design in the motor, preventing heat from being effectively dissipated. As a result, the internal temperature of the motor increased during extended operation, impacting its performance and longevity.

IV. Solutions

(1) Noise Optimization

  1. Gear Design Improvement: Replaced spur gears with high-precision helical gears to optimize the gear meshing angle and reduce noise during meshing.
  2. Sound-Insulating Materials: Added sound-insulating materials, such as rubber pads or sound-absorbing sponges, inside the motor housing to absorb noise generated during operation.
  3. Motor Installation Optimization: Ensured that the motor was securely fastened during installation to reduce housing vibrations, thereby lowering noise levels.

(2) Enhancing Torque Stability

  1. Control Algorithm Optimization: Implemented a closed-loop control algorithm to monitor the motor's current and torque output in real-time and automatically adjust operating parameters according to load changes to ensure stable torque delivery.
  2. Torque Compensation Module: Integrated a torque compensation module into the motor control system to dynamically compensate for torque output through software algorithms, reducing torque fluctuations during startup and shutdown.

(3) Heat Dissipation Optimization

  1. Heat Sink Addition: Installed heat sinks on the motor housing to increase the surface area for heat dissipation and improve cooling efficiency.
  2. Internal Structure Optimization: Redesigned the air flow channels inside the motor to add ventilation holes, ensuring effective heat dissipation during operation.
  3. Thermal Conductive Materials: Applied thermal conductive silicone to key components inside the motor to quickly transfer heat to the housing, further enhancing cooling performance.

V. Implementation Results

(1) Noise Reduction

After optimization, the motor's operating noise was reduced from 50 decibels to 35 decibels, significantly improving the user experience and reducing noise pollution in residential settings.

(2) Enhanced Torque Stability

Torque output stability was improved by 30%, resulting in a smoother curtain opening and closing process and a noticeable increase in the device's operational efficiency. The long-term stability of the motor was also enhanced.

(3) Improved Heat Dissipation

The motor's operating temperature was reduced by 20%, eliminating instances of overheating and automatic shutdown, and significantly enhancing the device's continuous operation capability.

VI. Conclusion

By addressing the noise, torque stability, and heat dissipation issues of the A58-3650 DC motor, the R&D team successfully resolved the practical problems encountered in application, significantly enhancing the performance and user experience of the smart curtains. These improvements not only solved the immediate issues but also provided valuable insights for similar application scenarios. Looking ahead, with continuous technological advancements, the A58-3650 motor is expected to play a significant role in more smart devices, bringing greater convenience and innovation to people's lives.
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Shenzhen Jinshunlaite Motor Co., Ltd.

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Tel: 15818723921

Fax: 86--29880839

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